ML7 refurbishment - Part 1 cleaning and repainting
The starting point was to dismantle the lathe to see what was what. A gallery of pictures below shows the process better than any words...... although the text is added below.
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MYFORD ML7 Refurbishment I had to opportunity to purchase a 'scruffy' ML7 so I thought I would take a chance and buy it with the opportunity to tidy it up then see whether I Myford Refurbishment 23rd February 2008 Session 1 After spending some time previously making the new bench , I started by stripping the lathe to see what was what. Then I tackled wiring the motor up I then spent the rest of my time in the workshop sanding and cleaning the electric motors case, and then spraying it in primer. That was it for today. Time spent today 2 hours. Total to date 2 hours. ==================================================== 24th February 2008 session 2 Today the undercoat sprayed yesterday, was sanded down and the after cleaning, painted with the green Myford paint. I will repaint all of the lathe Time spent today 30 minutes. Total to date 2hr 30 minutes. ==================================================== 25th February 2008 session 3 Had a brief 'preparatory' session today whereby I sealed the edges of the tray on the new bench, ready for a protective coating of Hammerite Time spent today 30 minutes. Total to date 3hrs ==================================================== 26th February 2008 session 3 Today I managed to paint over half the top tray now the sealant has hardened. Next time I will be able to locate and drill the correct location before Time spent today 1 hour. Total to date 4hours. ==================================================== 5th March 2008 session 4 With the lathe came the basis of the Dewhurst switch, housed in a rather makeshift housing of wood and aluminium. I decided to make a new housing, The design requires 4 pieces of sheet steel. The top and bottom pieces [photo 2 on the left],the back, and the main body. The tops were cut using my Onto this rolled main body, the top and bottom cover will be welded or riveted. To ensure they were a matching pair, I used a file by drawing it over I am at the cutting out stage at the moment, and will treat this as a bit of an infill to the Mills diesel engine construction. Time spent today 1 hour. Total to date 5hours. ==================================================== 19th January 2009 session 5 Since selling my much loved ML10 and seeing it depart on Sunday, I have been spending the proceeds! When stripping the ML7 lathe down I found a When my brother very kindly moved the ML7 into the main workshop last week, it started a train of events leading directly to Sundays sale and funds Here is a picture of what she looked like in the beginning………..(surprised to see it was February last year!) When stripping the lathe down I was surprised that some parts were very worn whilst others were in good condition. Which leaves me to believe that With a list of the parts needing replacement I phoned Myford and spoke to Malcolm in their parts section, giving him my order. Whilst on the phone I Following the Myford call, I then phoned a company that supplies inverters/converters and electric motors. My ambition is to have an accurate lathe There are a couple of shafts that I will have to have a closer look at. They are the lead screw end. Initially I thought that they were very worn So the current situation is a lathe completely stripped down and major items are hand painted Myford green. A list of new parts have been ordered The digital readouts will have to be in phase two (need ot raise the remainder of the money - more expensive due to the £’s slump). Hopefully tomorrow there will be a few photo’s showing the reassembly process. |
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20th January 2009 session 6 Today it was back to the paint brush and a bit of a surprise. The high quality paint brush I had been using did ok, but I thought the paint lay on a Yesterday I ordered the new electric motor, inverter and remote control and today it arrived! Good service so far. The package also included three The latest edition of Model Engineering Workshop arrived yesterday and included an article of a rev counter that seems a possibility for the ML7. After the excitement of unpacking the new motor I then hunted around for the pulley that fitted the old motor. Needless to say the bore of the With so many parts laid out around the workshop drying and the new motor unpacked, I thought it was time for a cup of tea, and a new list of action I am now waiting for some handles from RDG Tools online and various items for Myford themselves. I must be honest I am really enjoying this refurbishment project, surprisingly so. I am treating the ML7 as a big set of castings and it's a good way List of actions for Myford ML7 refurbishment 20th January 2009 So look back and in and see how I get on with reduce, then adding to the list!
26th January 2009 session 7 Well I seemed to have missed writing up a few sessions, either that or progress has been slow. Perhaps it's a bit of both. Using the list above, the The countershaft then became the focus of my attention. The first task was to remove the old iolite bushes, so a brass drift was turned to allow the Putting the countershaft to one side I decided to fit the new electric motor and do the wiring needed. A new pin for the motor bracket had to be New grub screws were then cut to size and fitted to the aluminum casting(s). Having attached the motor bracket the new electric motor was placed
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